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Frank Miles wrote:
Tektronix was, during that time, strongly discouraging all new designs from using tantalums. IIRC they had been taken to court over a case in which a 465 'scope (the original, not the plastic follow-ons) had spontaneously ignited and had resulted in an expensive fire. Forensics revealed that a tantalum power-supply bypass cap had started the conflagration. The drive to reduce tantalum usage was driven primarily by this liability issue, more than component cost. If you wanted to use a tantalum, you had to justify its usage to the component/design review committees -- which wasn't difficult if you had good reasons and your design was solid. -frank (ex-Tekie) I was there at the time, too. Tantalums were essentially verboten unless the source impedance supplying the tantalum cap was at least 3 ohms/volt. That's because it was found that the short circuit failure mode was aggravated by high inrush current, so the source current had to be limited. One of the chief reasons we had been using tantalums in the first place is that they have very good bypass characteristics up to quite high frequencies -- so a single capacitor could handle a very wide range. When the source impedance was high, the capacitor didn't need to be so good in the first place, and of course adding a physical resistor in series with a supply bypass pretty much defeats the whole purpose. Consequently, the 3 ohms/volt rule pretty much eliminated tantalums as a viable choice for most applications. Fortunately, it was at just about the same time that very big improvements were made in aluminum capacitor technology. As the aluminums shrunk in size, they became much better at bypassing higher frequencies. So they took over from tantalums pretty rapidly. There was a glitch for a while, though -- boards were being cleaned with Freon at the time, and it was discovered that Freon could migrate past the seals on some or most aluminum capacitors and corrode the aluminum, leading to poor reliability. The solution adoped by some manufacturers was to add a rubber seal at the lead end of the capacitor. That increased the length of the leads between the outside of the capacitor and the inner body, increasing the lead inductance and decreasing the capacitor's high frequency bypass capability. . . but that's just another example of the day-to-day problems an engineer faces and has to overcome. Incidentally, I got a Tek 1502 TDR on eBay not long ago. It had a shorted tanalum power supply bypass capacitor. A couple of other anecdotes -- A time base plugin I designed had gotten through the entire extensive pre-production test phases, accelerated life tests, etc., and was in pilot production. I walked past the production line technician's bench every day, and began noticing several tantalum capacitors of the same type in the replaced-component box. They had come from a sweep circuit I had essentially copied from an instrument which had been in production for some time. Puzzled, I analyzed the circuit carefully, and discovered that at an extreme setting of one control, the tantalum cap could have a very small reverse voltage applied. I modified the circuit to eliminate the possibility of any reverse voltage of any level, and the capacitors quit failing. Servicing data from the instrument I had copied the circuit from showed noticeably reduced reliability of the capacitor, also. The lesson learned is that tantalums won't tolerate _any_ reverse voltage. If they don't fail immediately, a disproportionate number will fail eventually. The other anecdote involves a QRP rig. As a crude reverse-voltage protection, I had reverse-connected a 3-watt diode (actually, a 36 volt zener I had lots of) across the power supply terminals. My battery supply normally had an-line fuse which would blow. Just before Field Day one year, the fuse holder broke and I didn't have a spare in the junk box. I'd never blown a fuse in 20 years of Field Days, so went without. The battery was a 12 volt, 5 Ah sealed lead acid unit, capable of a few hundred amps if shorted. As I'm sure you've guessed, that was to be The Year of the Reverse Connected Supply. The wires to the battery immediately melted out of their insulation, burning some holes in the tent floor. I managed to disconnect the battery without getting burned and before a real fire started, and checked the damage. The rig's (recently installed) power switch was fortunately off, so the innards didn't get any reverse voltage. The diode had gotten so hot that the plastic case had fractured and probably burned -- it was gone. The diode's solder joints had melted, and the two separated diode leads were dangling. But there was still a dead short across the terminals -- a small 6.8 uF dipped tantalum capacitor was also across the terminals, and it had become such a good short that it hadn't gotten hot enough to explode. (The power supply wires were something like #24 or #26, so they'd limited the current.) My guess is that it went short just as soon as the diode opened, and made a better quality short than the diode had. The fuse is now back in place (along with new diode and capacitor), so of course I haven't reverse connected the supply since. Roy Lewallen, W7EL |
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